Music systems, compacts and portables,vinyl record decks then Audio Cassette and tape players

The following are repair briefs for various 
equipment.The information is directed
to technically competant repair engineers.Generic terms have 
been used to make this info less model specific,eg terms like 
replace transistor Q123 have not been used.
The equipment is Music systems, compacts and portables then Audio Cassette and tape players. 
I would be interested in finding 
any other repair listings on the internet structured as i have 
done ie intended to be less model specific. For convenience using search-engines, 
use keyword divdevrep to target these files.

There is no point in contacting me about any of the following, the 
repair job may have been done 15 years ago .
I cannot clarify or enlarge on any of the following.



Should the location of this file change please use the keyword "divdev7" in a search engine to find it again

Music Systems, record decks

AIWA CX770K Midi Neither tape unit working L play only dislodged sub pcb with contact switches.R rec/play bent location spiggot that passes through hole in cassettes and the normal/reverse switch was separated and jammed so extended yoke of the join so it could not be forced out of contact with the actuating lever. Aiwa LCX 352 midi system The owner wanted to plug a vinyl deck into this system. This conversion probably is applicable to most modern systems with no phono/cartridge level signal input. Equalization is perhaps off and the signal level is probably a bit too high so next such conversion i will probably add a couple of presets in the signal line. Where the tape deck play signal lines from the tape head join the screened leads to the main pcb solder in a pair of screened leads and take to the rear of the machine and an extra pair of phono sockets. Plug the record deck signal leads into these and select tape mode. To defeat the tape protect system butcher an old cassette by cutting the tape and use this as a dummy.The tape protect in reverse play on this m/c will not cut in.On other machines that will detect in play and reverse play it would be necessary to open a cassette,strip out all tape and leaders,loop around both spools with a rubber drive band. Aiwa ZVM260 Compact HiFi Disappearing main display and tape problems principally but also intermittant CD problems The intermittant display problem was (YET AGAIN) heatsinking from large metal parts insufficently soldered in the original flow soldering operation. This time some of the pins to the cold-cathode display. On switch on there is tape solenoid clicking in and out for a few seconds but no tape operation. The LH tape mechanism had failed to retract due to stretched drive band and the owner had forced open the door breaking the plastic flap catch. To replace the bands first remove the top CD unit firstly upwards at the rear clearing the optical output. Mark the track of the two tape main bands as completely different tracks. The RH tape drive band comes free easily but the LH is retained by one of the motor pillars. This is just a locating,not a fixing pillar. Force the motor on its flexible mounts to expose the small pip at the end of this plastic pillar and with a hacksaw blade (no handle) cut off this pip. The band can then be pulled through. Otherwise the whole machine has to be taken apart to remove the twin cassette section,who designs these things?. Use a couple of hooks to replace the band around the motor spindle. To replace the flap catch. Use a 1/4 inch male spade connector as soldered to PCBs. Cut off one of the 2 mounts and bend the remaining one to a right angle, bond into the carrier plastic with plenty of hot-melt glue string. Accurate posiioning is required otherwise the carrier will close but not open when pushed in the normal area. The CD problems were 1 Overnight occassionally the CD drawer would open of its own accord. Packed out the 1,2,3,4,5 etc switch board between it and the casing. 2 Occasionally would not read a CD, could be any CD. Resetting via the disk change switch would usually clear for the moment. Cleaned the lens and adjusted the preset resitor next to the laser. Accurately measured the ohms across the ends of this preset and noted the original reading on the m/c and adjusted down 5 percent. Before replacing the 3 white foil ribbon cables especially the very thin one in the CD unit bind the ends with upholstery tape to reinforce. Beocenter 2100, type 2442 , 1985 Phones output but not always at power up, speaker output. Fuses under the cover near the mains transformer ok. 23V to the relay failure. Originally thought TR7 in the ps for the protection circuit/ output relay driver circuit, but I don't have the manual for this one. The emitter needs to rise to about 2V with 4.8V on the base before the relay driver changes state It is between TO92 and E-line, slightly smaller than TO92 with a small flat on the curved surface It in pnp , marked 115 4XF so not BC115 or 1154 or 2SB115 or 1154 Would it be short for B&0 number sequence preceding with 8320 so 8320115 ? and 4XF as date/batch code for 1984 perhaps Its that sort of size of a DTC115 , digital transistor, but about half the transistors in this music centre are of that size so unlikely. Also that one and the others check out "double diode" test with DMM as normal pnp transistors. Used a BC558 with crossed-over legs. The other ones npn etc, in this unit, of this small format, are lablelled 603 and M21 instead of 115. Looking in the Beocenter manuals that I have, I cannot see this package in the the gallery of transistor packages used in those units. Perhaps they were a Danish manufacturer of mid 1980s Problem area was around TR8 with undefined biasing from the pa line. Touching this line would trigger off state of relay to on. TR1 ? in the pa was off wheras presumably it should be just on giving about 0.4V at the collector. More than 0.6V or less than 0.2V in pa failure then the relay driver goes off. Measured voltages , approx, as B,C,E TR1 23.4,.04, 23.4 TR2 0.23.4,0 NPN TR3 0,-23.6,0 PNP TR4 -23.7,23.5,-23.6 NPN 0.4V remained, after power off, on the back to back pa 47uF caps C1 and C2, so replaced, and also the 3 caps around the protect circuit, not all 10uF Added 2.2M from 4.8V to TR8 base and 33K over R23 which otherwise just had in effect 100K to ground, to give a definite bias so then the electrolytic could charge up and turn on the relay after the hold-off time. Copver screw removal sequence marked on the base. To inspect the power transistors slide the heatsink downwards. The release cattch for the top cover aon the radio side had been pushed in fully. Flimsy plastic. Removed and added a couple of small cable tie hoops to push the spring away from the plastic "spring" retainer so the metal spring cannot over-ride it and more closure force to the pin as it was a bit bent and bound on the holes. The instructions on the base only tell you to push in this pin , not press on the grill section at the rear 1.5 inches in from inside to release the 2 rear catches before sliding forwards. 16V ac on the one remaining front panel bulb. Earthe plate between mike socket and motor , the separators degraded and metal very near the contacts. If looking in the radio area mark the LED position of the dial scale on a known station before releasing the radio pcb , so can realign on reassembly Beogram 3000, type 5228, 1973 Very erratic speed and an annoying clicking noise. Slide perspex cover hinge section rearwards to remove. The legend on the selector central push pad had worn off and it confused me how that action was initiated, not seeing that as area as a knob. Cured the main problem of erratic speed - solidified grease on the main swing arm , stopping the thin moulded hard rubber?(dark brown colour) edged pulley, freelyly swinging and engaging with the stepped conical motor bobbin with the pull in of the main platter drive band. Remove the 3 screws and 1 nut and then release the spring on this drive mechanism. Release the wire "U" clip between the twoo sections that changes from 33 to 45 rpm. Remove that cam with the black plastic cylinder. But there is an intrusive noise associated with this pulley , once a revolution. Nothing obviously wrong , no cracks, bulges or anything on this edging. The noise is from the intermediary idler pulley, once per pulley rev. The noise was coming from the (forgotten the mechanical name) the pulley that engages with the pin/plate that is moved on adjusting the speed. That shift pulley coaxial to the idler pulley, so moving the idler up and down the drive cone bobbin, for speed change. There was a tiny nick and gouge out of the aluminium of the active surface of that "gear-box shift" selector pulley so flexing the plate on each revolution. But at least I know that moped inner tube dodge works should anyone faced with a broken /totally worn thin idler edging. I run a strip of stretched moped inner tube around the edge and glued in place to see what happens to the noise. Measure 1500 ohm outer and 1520 ohm inner in my notes but forget what that refers to. When power take off for the arm lift then the belt fell off as too slack. Platter is 660mm circumference, ideal band is probably 650 mm but old stretched band was 680mm. The only near suitable band I could find was a "halved" lorry inner tube band (see tips files) 580mm x 1.5 x2.5 mm rough surface to the outside. Combination of too tight a band and the increased diameter of idler pulley meant the 33rpm was unattainable on the knurled knob adjuster. Had to introduce a TO220 tab plastic insulator under the point of that adjuster to push the setting plate further away and higher speed ratio on the cone drive. Bang and Olufson Beomaster 1200 tuner / amp Very bad volume control on one channel. Another cherished heirloom.Problem due to a broken pot slider. To get to the relevant area to desolder the pot.Remove the 3 screws on the base to remove steel base panel after desoldering earth clip and mains wire to on / off switch and four signal wires. Remove three of the most accessible of the 4 aluminium L bracket pieces that engage with the rectangular wooden surround and remove. Remove long rear plate ,disengage from the 2 Din sockets.Remove black plastic front grill with the main switch lever pannel.Remome the small aluminium slider area cover pannel held by the 2 spring copper clips.The errant pot had a graphite insert that had broken or dropped out.Compared with other pot it was a conical shape just pushed into the metal of the slider.Replaced with a mushroom shaped pip from a cermet preset but diameter slightly bigger than original so opened out metal of slider.Placed in position temporarily held in with a bit of gummed label to be able to turn over and put a dab of glue on the other side of the graphite pip. Reassembled pot and glued along seem. Beocenter 2200 no scale illumination. (1984) Original T1 1/4 format bulbs were probably 13.7V could only replace with dimmer 15V ,40mA but gave sufficient illumination. Instructions for removing casings are under the deck platter. To slide cover off the scale area push the release pin near the dust cover right hand hinge. Mains switch is at the tuning control. Screw down at least 2 of the deck anchors (under platten) before moving the m/c to avoid bashing the stylus as flops around a lot. Deck operation commenced by sensor to detect presence of a record. In effect weighs records to set the radial start position. 10 to 70gm for singles and >80gm for LPs. For anyone bodging a coupler for a standard pick-up the pins need to be .6mm diam and signal lines are 12 o'clock left ch and 3 o'clock Right ch,looking at the sockets on end of arm. No tape functions - just a relay click noise. Stretched drive band jammed against cover plate. Mark all 4 connectors before removing. Replaced both this flat belt and the square belt with the strange path, only 1/4 round drive pulley and both nylon pulleys. Beocenter 2200 , type 2422, 1984 Missing cartridge and stylus, 120 GBP for a new one which a pensioner was not going to pay. Beware aluminium platter only resting on centre, remove before turning over Remove black plastic covers at the main hinged lid to reveal fixing screws. Undo base screws around deck area and the internal ones to release the inner deck surround, lift away after releasing the 2 leftmost screws, marked "A" holding the static rear of the top cover. Replaced with a standard moving magnet cartridge with elliptical diamond stylus. The cartridge did not properly sit in its stowage housing because larger . Also heavier ,Added 25 gram strip of lead to the existing 65 gram. The weighing mechanism at the centre of the platter needs about 100 gram to register as an LP, without it, registers as single. If more anti-skating force is required then a light spring attached rearwards to the final lift activation wire , that also doubles , by deflection as anti-skating corrector. The rearmost slide bar is the radial tone-arm posistioner which needs a bit of spiral cable wrap around the vertical white pillar to reposition the initial drop position with added cartridge. The nearer long steel bar rotates slightly to operate the arm lift. Switch off at mains in mid play position if required to work on mechanism. The cartridge stuck to the small socket housing on the end of the tone arm. 4 turned pin IC socket pins bent and fitted in the sockets , wired back to cartridge pins through a small plastic ring to take up space above the existing cartridge socket housing. Bit of double sided tape to assist initial placement of new cartridge. One small cable tie around all and tightened and then when finally angled posistioned correctly lock in place with some dabs of epoxy glue. Paint black and stow the signal wires to try and improve the appearance. In play mode the two main headers, DC 11.3,0,0,10.3,0,0,0,0 42,0,0,0,0 B & O Beomaster 901. All 3 indicator lamps had eventually failed so no mains-on indication and of course some awkward wedge ended bulbs. 5mm LEDs are just the right size to go in the recesses if the plastic skirt is cut away from each LED. The original bulbs are 12V,30mA so place 120 ohm,2W resistors in series with each LED. Adjust the 2 presets on the board associated with the two matched tuning indicators. The Green indicator needs a strong radio signal to come on. Beomaster 3000 - 2, type 2402, 1971 Nasty buzz from both speakers even zero volume. Failed 4700uF, 70V capacitor on 60V line, middle of the 3 main electrolytics. Only 40V Dc and 16V "ac on DVM" and buzz in test piezo earpiece. Bush 9100, 1985 Cassette stuck inside. Stretched band so not fully engaged tape. Whine on playing could be due to mis-positioned Rec/Play link wire , also dropping out of play signal one or both channels. Testing needs all cables connected except the aerial one. Presumably cannot be turned from standby to power without the remote. Bush MC A1/A micro audio CD stops playing soon after starting. Remade all solder joints at BA6898 and all connections up to the platter motor. Survived me creating a solder bridge at the IC between the 2 output lines. What I thought was a solder bridge between pins 6 and 7 was a half-hidden power rail pcb track cutting this stopped sledge,platter and focus drive. Probable cause was one of the header connectors so soldered 6 way lead instead of connector as a connector on either end anyway. Sluggish tape rewind - replaced the second drive belt with a larger section one. Whole unit comes apart quite easily and is workable on in dis-assembled state. Curiously there was a hand scratched message in oriental script written on the aluminium faced cardboard under the CD processing board. Bush MRC110 Radio /Cassette Clicking noise in play Irregularity on the floppy intermediary cog,flexing making it worse. Bent the end stop to the activation radial arm so not deforming the cog so much. Bush MC A1/A , 1997 No movements or laser light , totally dead CD player. Just -- in the display. Function sw and door latch sw ok. Plenty of 5V etc supplies around on the chippery. Crystal and ceramic resonator have oscillation. All 4 channel motor/focus driver o/p at 3.8V, all 4 inputs at 2.1V, disable is set off ie operational. Pressing all sm chip leads , no change Swapping laser and carrier/motors section with another one laying around, the same zilch. No dodgy electrolytics. all BA6898 i/p 2.1V, all o/p 3.8V. Failed to get it working, too old and basic to bother any further. Dansette valve amp record deck 1959 or so "Bermuda" as Major de Luxe of 1959 , BSR Monarch deck Had been in a loft for years. Remove the 8 screws around the deck base and pull the metal deck through the hole. Original Mullard EL84 tested good gain,no leakage, and all else checked out. On powering there was amp hiss and crackle on turning the worn out vol control. But stroking the stylus with fingertip produced nothing. Wiring between pu and vol control is fine. Putting the output of either pu LP or 45 to a scope and touching either stylus produces absolutely no signal at 2mV per division. Make of rotatable pu Ful-fi , Made in England, number TC8S , and TC8C and TC8RS for the stylii. Connected to the valve grid via 1M vol pot. Let this be a lesson to anyone in the UK - DO NOT store Rochelle crystal cartridges in lofts or sheds. The crystal must be hygroscopic. After removing the copper rivets (used flute section of small end mill to avoid the rotating rivet problem with drilling out rivets in plastic) and separating the 2 main parts, the problem was obvious. I just managed to move the parts apart enough to photograph before the active part fell to bits, lightly probing with a pin it was the consistency of dusty paste. (1 mm graph paper) http://www.diversed.fsnet.co.uk/ful-fi1.jpg Left section is the cover, slid sideways, and the R section, on a nylon nut for focus, is inverted, part of the "crystal" with angled ground strip that touches the central pu pin (common to the other pu) to the outside, along with the signal pin for that pick up. The other pickup , not seen yet, but will be the same state, is under the central view. The brown part is the rubbery material that engages with the crystals and stylus shafts. Plenty of copper carbonate corrosion inside. The remaining parts of the yoke, styli etc http://www.diversed.fsnet.co.uk/ful-fi2.jpg I assume piezo-ceramic is not prone to this problem over 40 years. I reckon it is possible to convert piezo cartridges. I have dozens of later N.O.S Sonotone mono pickups, but have never looked inside one. http://www.diversed.fsnet.co.uk/ful-fi3.jpg The central image is the active section. Not obvious in pic but the 2 vertical sections are each metal/piezo-ceramic/metal sandwich like bi-metal strip in fabrication, set in quadrature, so a pair of pickups, but electrically combined for mono output. So although these are pinned out as mono, just rewiring the innards and adding a pin would presumably convert to stereo. Electrical contacts are via fine sprung strips set in a black rubber pad like the white one shown, there is also another such black block removed, they hold in place in the casing. The lower creamish joining part is the plastic cradle/saddle for the stylus shaft. Cutting down the rubber pads a bit and sorting out some contacts and gluing in the ful-fi casing will probably work, whether capacitance etc is wrong I'll wait and see. The kid's clothes peg, 1 inch long was just right as an insulated clip to hold a pair of contacts, temporarily, to check on a scope. The circuit is minimalism, as in the Newnes 1959 guide for Dansette Major de Luxe. A triple cap can, 2 other axial caps, 2 Rs, rectifier , 2 pots, EL84, mains and o/p transformer. I took another Sonotone apart. I had not lost a silver spring from the other one, only one active element is used so 2 wires only. I will try lashups as series and parallel trying to determine which gives most signal/ most f range. I decided to take a skew view before wiring in http://www.diversed.fsnet.co.uk/ful-fi4.jpg 2 rings of green silicone rubber sleeving to take silvered wires before dabs of gummy glue. One black rubber pad chamfered to rest in the top cover, yellow-white rubber pad cut down , orginal brown rubbery moulding that enclosed both original rochelle crystals and extensions to both stylii saddles. The saphire of the original remounted ( coded yellow and green) stylus is just visible to the top and right of the brown section, through a gap in the white plastic casing. The original small plastic stylus saddle went quite neatly through the hole for the original rochelle. The now unused second brass screw mount for the other stylus and its corresponding saddle rest flat, on the brown section, is visible on the lower edge. Decided to wire in only one active element of the Sonotone and also to have more space to play with ditch the 78 option and just use 2 of the original 3 pins and plates to the outside. It is very critical on signal generation on how much the rubber supports are compressed, I may cut the thickness down a bit if the sound is ropey. It would probably be possible, in space terms, to separate the 2 sonotone and mount one either side and retain double stylus, rotating function. Decided as the original Sonotone was neatly anchored at the saddle end then mounted to try with just the black pad in place to avoid damping the piezo. Googling for what a Rochellle crystal should look like I found someone else has gone down this route http://www3.sympatico.ca/belanger.eric/Radios/cartridge.htm completely different internals I had to abandon putting piezo element in the original cartridge housing, not enough output. Sliding a cable tie lightly and easy direction over the stylus gave about 100mV , wheras doing the same over a complete piezo, ie vibration not having to go through a load of brownish rubber gave about 2V pk-pk output with the cable tie. Adabted the yoke to be able to slide in piezo pick-up ,retains the little 78/LP flag , and can rotate but no second stylus, and is shrouded in the arm so nothing shows in normal use. Nylon ring on either prong of the yoke, to engage with the Sonotone , bound with PTFE and swathed in hotmelt glue. On removing PTFE made a reasonable mount into the yoke held by the original headshell part. 260R mains primary // motor, 350R + 0.6R (heater) secondary Speaker 2.2R o/p transformer .5R with speaker and 385R Original cartridge 5gm , replacement 3.5gm. Feeding 1KHz , 200mV directly into th evalve gave reasonable sound level. Squeal on motor drive - removed the large ciclip to remove the platter and small circlip over rubber disc pulley and cleaned out. Replaced the selenium rectifier with 1N4007 mounted on a 20mm fuse holder as a standoff, as original was introducing a lot of hum. Digression on trying to find way of testing Using 9V battery and 300 ohm dropper shows near enough 9V over the rectifier, how high V do you have to go with a good one to check it ? Are there safety grounds anyway for changing to a 1N4007 or so ? Single element rectifier Siemens lazy S logo Made in Germany 2250c50 Kc 0.6e 11/16 1979 Siemens databook and E250C50 were still listed, rating only 200V, 20mA I removed and tried on a bench supply thru 330 ohms. Took to 25V and read over the rectifier 25V, powered either way So replaced with Si At switch on the DC at this rectifier 300V dropping to 220V when fully on. On removing/replacing the rear connectors make sure you don't short the bare ground connections to something. The "stereo" output is just cartridge output , presumably there for a later up-coming technology of 1960s conversion to stereo cartridge Ferguson 3T13 portable stereo No mechanical tape functions. Yet another m/c well past its use-by date that the owner cannot part with.The drive belt had dropped off due to one of the 3 rubber suspension grommets for the motor dissolving into chemical slush the remaining 2 would soon have gone the same way. Fisher FM-M75 tuner of a M70 system Intermittant loss of station Not enough clearance between front panel switch pcb and the fascia intermittently allowing the channel 1 switch to activate so pack out the standoffs a mm or so.Also the display lamps needed changing but requires 16V lamps so bodged up with two sets of seriesed 9Volt lamps Freeplay Freepower Bayliss South African clockwork radio , no tuning possible. Dial unscrewed from the tunning cap. Due to mangling of polythene sheet dialectrics crumpled up inside so it looked like crazed plastic on the tuner clear plastic casing. Presumably shorted vanes on AM . FM tuning was ok. Fixed dial piece back to the shaft of the tuner. The recess was ground up so had to melt 2 pins into the remaining plastic to mate with the flats on the brass shaft. Didn't bother replacing or remaking tuner cap as only a crude radio. When dismantling only remove vol knob, the tuning knob is set from inside under the 'dial cord' mechanism. Also the aerial was broken. To access this area requires removing the clockwork generator. Before removing cogs hold back the residual torque even when run down. Presumably this generator is demand led in effect via motor/generator back emf/torque. High output the 'escapement ' runs round fast and slow for low level or off position. Extra electrolytics may be useful as output is highly erratic - well on this one it was. Radio uses Telefunken U2510B IC Gemini PT1000 vynyl deck 1997 Cosmetic copy of Technics SL 1200 /1210 . Never mind the quality feel the weight -big lump of steel in the base . Powered up but failed to rotate platten after being moved between premises. Owner lifted off the platten and changed 230 V to 110 V and blew the fuse. 1 amp fuse blown in IEC socket. Replaced with 160mA as only a 20W transformer inside. Back to the original problem changed the on/off microswitch but probably only needed packing out between knob and switch lever. With platten removed but running set on 33 moving very jerkily so could turn upside down. DC Voltages on main microprocessor board ribbon cable were 0,10.8,6,.1,.1,.1,2.5,0,.1,.1,3,2.8 to 3.4 varying,5V General vinyl deck problem. New owner of deck reported signals ok but hum problem on both channels. Mag cartridge but DVM reading between signal and shield of infinity. 400 ohm between signal and sheilding of other channel and vice-versa. Someone had crossed the wires between cartridge output and tonearm connector so neither signal line sheilded inside the deck. Goodmans 2725R 3 CD midi 1999? Loss of one channel on radio and much later total failure. Radio problem probably at manufacture , the radio o/p lead part guillotined , screening wires half cut and most of one conductor cut so eventually one remaining filament failed. One 2A fuse blew because of failure of one 1N4002 bridge diode. TA8216H uses a 1000uF,25V to block DC on each speaker o/p. 4052 for function switching? on power board with 7812 (15 ohm or so to ground normal), 2SD882 and TA2078. Mark all lead plug/sockets before removing The mains lead/transformer joint is as manufacture. Remove 2x3 side screws to remove phono deck Remove 2x4 side screws to remove CD unit Goodmans 4460 mini hifi CD drawer not working and failure to skip tracks Excessive lubricating grease on the gear train to the tooth rack had splattered upwards onto the rubber drive belt,so cleaned and replaced belt.The Cds would play whole side but not be able to skip one or more tracks.The final part of the radial positioner is a plastic tooth rack held by 2 flimsy strips of plastic to act as a week link,at end stop etc the rack would disengage from the pinion.I suspeced weakening of this plastic rather than build up of friction on the laser carrier. Straightened out some small spring wire and fixed 2 lengths to the existing 2 plastic mounts with hot-melt string to beef-up. To align tray mechanism hand crank the gears until the tray is in and the platten clamp is about to move is where the tray is free to move in and out disengaged from the rack. Goodmans CM80 approx 1968-1972 music centre (no ICs,2 AC138 brown rectangular and tubular Rs and Cs). Lenco Swiss transcription deck that is half the weight of the whole unit. Crackly volume and rubbing tuning knob. To remove top undo 4 + 1 wood crews on base. Tuning prob was sub plate behind front pannel out of register with tuning shaft and filed back. To recondition dual and compensated pot,demount,bend back 4 alloy tabs at D shaft end. Remove associated track. To remove other cover use a heavy duty point such as an old dartboard dart to prize back the relevant 4 tabs. Someone had previously replaced 2x MJE2955 with TIP43C with swapped legs on one channel and no problem there. Grundig C9000 old portable radio /tape. Blown pass trannie in ps marked GD 361 which is Grundig special 22V,4A. Replaced with BD787. Balance control worn out. Made by Preh very odd single track pot. 0 to 40 percent of track 200K ohm ,40 to 60 pc insulation then 60 to about 100 pc 200K. Wiper pin not centre pin. Dismantled and wiper not very flexible and contact had totally worn down tracks. Cut one of the wiper arms to reduce springing and bent contact to new part of track. Small 5mm black plastic 4 pinned IC marked 720 in ps probably dc to dc converter for tuner pin 1 9.5V,pin 2 0V,pin 3 33V,pin 4 9.5V. To refit body to case move the tape type slider to mate with innards. Goodmans CM80 Very low level sound on one channel and then distorted if increased the vol. All DC levels match between channels and DVM tranny checks ok but lack of charge hold on large electrolytic. Failed to o/c 3300uF,40V capacitor between speaker line and junction of the 2 low ohm/high W droppers that look like silvered mica caps. Don't know if over-heated or plastic/plastic welding over time but the cap plastic covering was 'melted' into the P clip. Headshell connector problem. Vinyl deck headshells - severely corroded wires and absent connectors for the 4 wires connecting to the 4 pins on the cartridge. The only replacement for these channel profile connectors I could think of was the phosphor - bronze sliding contacts inside of basic slide switches. Broke apart a few such switches to rob the contacts. Slid on the shaft of a jeweller's screwdriver and cropped off the contact section to leave a channel and soldered fresh coloured wire to one end Hitachi SDT118 music centre No tape transport. Misaligned leaf switch in line with the motor under the tape unit . HITACHI TRK 8080 Intermittent loss of one channel then no transport Someone with sentimental attachement to this 20 year old ghetto blaster wanted it repaired.The channel loss was due to corroded/distorted contacts on the phones jack socket and the motor was totally defunct.This mechanical flywheel governed motor was replaced with an electronic governed motor with direction reversed by cutting tracks and reversing the leads to the actual motor and a change of pulley as well as adjustment of speed pot to get the right rpm. JVC RC X620 Ghetto blaster Intermittant then permanent no mains useage. Yet again poor soldering on the mains/battery diverter switch in the mains socket.Note some of the ribbon cable connectors on this m/c are push to release and others pull to release.Without all main case screws in place the tape cassette flaps will not lock down onto the decks. JVC RC828LB ghetto blaster,1977 Motor boating noise on one channel and to a lesser extent on the other. Due to excessive build up of black (copper sulphide?) on the endmost static contacts inside the input selector switch so braking contacts. This seems to be an ever more common occurance for old equipment kept in the acidified air of the UK for 30 years. Label the wires to the battery compartment when removing back. Unhook the plastic pivot connection to free the main board from the selector switch mechanism. Reconditioned the slide switch as per tips file. Problem closing the cassette flap due to wear on the take-up drive dogs allowing the spool of the tapes to catch on pillar of the take-up spool. Reduced the strength of the spring that lets the slidding drive dog push along the pillar. Heat on 2 bits of heatshrink sleeve to the bottom pivoting cassette carrier to raise the cassette a bit and toughen / bend back the 2 side springs to ] keep the cassette seated against the deck in FF and REW. Then 2 weeks later someone else with the same model needing repair. Again intermittant problem with the function switch and same black corrossion. Also problems with the phono sockets ,all very flimsy ,could only sensibly repair by wiring in some replacement satandard phono sockets in another part of the casing. While in there in FM radio mode DC voltages on HA11251 3.6,3.6,3.6,5.9,0,3.4,3.5,4.8 / 0,1.4,5.8,1.2,0,3.2,1.4,.7 AN 362 2.6,1.7,1.7,1.7,1.5,1.7,1.7,.1/ .5,0,.8,2.6,2.6,2.3,3.2,7 JVC RC838 Ghetto Blaster 1981 All sorts of problems due to spilt liquid. 240/110 V switch mounted not too obviously at mains inlet. Remove back then 9 internal screws and knobs to remove in one piece the speakers,front and 4 sides to expose innards All switches and sliders needed taking apart and cleaning. The Man/ Auto switch fouled so no record signal in tape record function. Same with the gummed up tape counter. Tape door return spring on wrong side of perspex lever so flap would not open. Design flaw means the tuning string rubs one of the chassis pillars. Wire at back of one condenser mike corroded away. No reliable tape transport function due to loose slip clutch with crack due to steel/ plastic expansion . Loose in 2 senses ,free to rotate on the steel shaft and free to slide so binding against the holding arm. Rotation meaning loss of torque at tape ends and sliding /rubbing leading to intermitant tape stop at any point. Marked the clutch position and demounted from the arm. Then with double action end snips held angled to the shaft in marked area made series of cuts into the steel then in reverse sense to give a crude knurling effect. The plastic slip disc would then locate positively on the "knurling".

JVC RC-W210 ghetto blaster Snagged tape,wrapped around pinch wheel Too much axial play on the drive spindle allowing the cogs driving the take up reel to disengage so removed plastic circlip around spindle and packed out with a couple of small running washers,modified the second tape unit in similar fashion. JVC RCX720 Portable CD/Tape etc One channel only for 10 percent of track of volume control To desolder the pot it is necessary to remove the LCD display board which disengages from the main PCB in direction perpendicular to the face of the LCD.Dismount the pot section from the motorised section. Fault due to slider prongs bending away from the track rather than worn track JVC R-S33L tuner amp Failure of one channel One of the HA1457 SIL preamps had failed at the rear of the graphic panel. Marantz TT2000 record deck Irregular speed To work on this deck upside down stick some tape around the central spinle of the platter,the inertia of the aluminium is required for proper running of the motor.The fault was a broken contact in the speed adjustment pot so affecting 33 and 45 rpm setting. Murphy (no apparent model number) portable CD/Tape/Radio Worn out tracks on all pots,vol,bal,and graphic. At least with these un-enclosed slider pots it is an easy job to put a pin in between the double slider contact fingers to open out to use a new section of track and lubricate. National Panasonic SG 2080 ,old music centre Loud interference on record. Failure of the long ,play / record function switch Panasonic FM15 tape/radio Poor switch contact on the wave-band switch. For short term squirted switch cleaner inside the mechanism and for long term formed one end of a tension spring around the black plastic actuator of the switch and anchored other end to a part of the pcb to force the sliding contacts to one side to make more consistent contact. Panasonic SA CH 74,compact hi-fi 1996 Broken mic plug stuck in socket,jammed CD mechanism Mark orientation of all removable ribbon cables before separating - foil type push and pull,wire type raise the surround before pulling on the cable. Pull front panel away from main body, 2 indirect connectors under the vol control. To get to mic socket ,remove 2 knobs ,remove display pannel then multi-switch pannel. Desolder socket ,drill small hole on underside and push remnant of plug back. This one has 5 separate platters to hold each CD. On entry the CD sldes along the bottom ,is elevated by the laser + spinner assembly and 4 flimsy 'ratchet' pawls hold the carrier in the elevated position and the main slide mchanism returns the carrier to the top of the stack of 5 after playing or along bottom to release/change through front. As a fall-back ,disabling the pawls and associated high level slideway the carrier will move in and out at low level for single CD operation without jams. Unfortunately a flimsey microswitch monitors carrier across the top and i won't know what effect non-switching of this micro will have until i rerassemble it all. Marvellous array of mechanisms all coming off the one motor drive . What sort of mind designs these mechanisms, rotary,rack and pinion, latches, compound slideways,translating and reciprocating motions? [ for anyone involved with this sort of thing or automata then this book may be interesting Ingenious Mechanisms for Designers and Inventors Volume I: Franklin D. Jones; 1930, 536 pp, illustrated, ISBN 0-8311-1029-5 ] Retrieved a displaced torsion spring from elesewhere in the casing. This biased a latch (at the rear) that engaged / disengaged at the point where CD carrier sliding along base changes to vertical movement of the laser + spinner and carrier. It looks as though a physically large but not strong torsion spring ,now missing, used to be at the centre of a long lever and quadrant cog that drives a lead screw to push a lifter of all the stacked CDs. Could not make sense of this spring, as to function properly ,seems to be the reverse action to what the anchor hooks would suggest. Finally under the front edge of the CD carrier slideway is a little passive latch that holds/releases the bottom-most carrier relative to the slideway. Fingernails pushed behind this cover and forced up and out will release it. This latch ,not obviously as covered,was out of alignment because the central plastic pin was broken- replaced with glued in nylon bolt after drilling a hole . Broken pedastal type of microswitch monitoring slideway limits. For these 2 uswitches with CD drawer out both are s/c, in between sw1 s/c and sw2 o/c. Drawer in both o/c. 2 uswitches monitoring laser carrier movement in play sw2 &sw3 s/c ,in between sw3 o/c,sw2 s/c at bottom position sw2 & sw3 o/c. Top slideway microswitch n/o Drawer motor 3 to 4 V for external powering or remove rubber band and turn large cogs by finger. On re-assembly intermittently powered down showing error F61 or FG1 ,probably dodgy ribbon connections as remade all and ok after that. Panasonic SG5090 monster music centre of 1978 Wavering sound on tape both in volume sense and sort of cross channel effect. The erase and tape/record heads have a plastic submount. The erase is anchored to the chassis by both screws. The main head for some unknown reason has the adjustment screwed into this plastic and the fixed one into the metal. The plastic had broken away. Dismount and fix a matching 2mm nut to the screw and glue into the plastic with bracing from a solder tag over the nut and glued into the main plastic. Use a shorter spring for the adjustment of azimuth. The scale side-illumination festoon bulb 12.6V,.38A was o/c and no replacement available. Made up serised oblong section LEDs in a bank of 2 by 3 giving a somewhat pleasing red illumination even if lower brightness. Broke open a barrel fuse and soldered an end cap to each end of this bank of LEDs to mount in the existing bulb holder. Perhaps should have added another 2x3 set at the other end of the perspex as plenty of power of course available compared to the original 5 watt bulb. Philips 22DC752 (752) car radio cassette Jammed tape Yet again an example of that silly band of plastic around the periphery of the main drive pulley was broken and jammed (presumably differential temperature change of plastic and metal). Remove all plastic,mount the pulley on a suitable block by drilling a few holes in the pulley,bolting, and centring in a lathe (the spindle is only mounted in a plastic insert so robust mounting is required). Cut a groove in the edge of the pulley..Compensate for change of diameter by adjusting the drive motor speed regulator.Similar fault on a Philips VC 600 ,how many thousands of these Philips units have been junked because of this design flaw. philips aZ 9020/05 Ghetto Blaster Intermittent power failure. Bad solder joints on mains input socket/ diverter switch and pcb. Philips ND 7500/05S portable cd/cas./rad Door closure problems on CD and Cassette Puny plastic bow-spring on CD flap closure had snapped. Find a light guage small compression spring that can wind on 1 turn onto the shaft of the flap closure nib allowing free end to bear against the back stop.Then hot melt spring to plastic shaft. One of the cassette doors had broken away but solution is applicable to most cassette units. The 2 plastic pins at pivot points on L and R side of the flap had sheered.Find 2 (in this case different sized) washers that will give a clearance fit to the static bosses on the main body of the unit. With door flap removed from the m/c hot-melt glue these 2 washers co-axially to the pivot axis on the L and R and reintroduce to the main body. Not enough space now to use the original torsion spring (that opens the flap) so either a long tension spring one end looped onto the curved arm near the pivot after making a small hole in the top of the arm to take the end loop of the spring ,taken round the pivot with some small diameter polythene tube surrounding spring in this area and the other end fixed to body of m/c.Alternatively a small compression conical spring as used on -ve terminal of battery boxes glued to the inside of the tape deck to bear against the tape carrier when closed will give enough opening to allow fingers to open the door. Pioneer PL320 direct drive record deck Erratic speed The pitch change pot needed attention or replacement. To remove the top cover around the tone-arm mount remove plastic plug at rear of tone-arm and undo the hex bolt to remove the rear extension to the arm Pioneer SX 700 Tuner amp Cracks and bangs ps fault Dry joint on 2SD525 Repairing vinyl record decks. Before looking at the innards remove the cartridge or at least the stylus, tie the arm to the suport rest/pillar. If not positively held also remove the platter. Samsung SCM 8250, music centre CD s often not playing, showing No Disc. When it worked then whole CD played Dealt with the usual suspects. Removed top clamp and tried with a heavier magnet clamp spinner while checking for laser o/p and focus/tracking action, then glued an 8gm washer to the original, cleaned lens with meths then cleaned off excess grease on innermost part of sled rack. Undid screw near the drawer motor , lifting CD unit and propping up the sliding plastic piece to give space to clean away excess grease that was likely to get on the band and replaced band. Sanyo MCD Z10F CD ghetto blaster Intermittant failure of fm radio. Dry solder joints at either end of one of the small fixed 4 turn rf coils next to the tuner cap. Due to the thick guage of the wire for this coil and its inherrant heatsinking the original (flow-solder?) soldering had been inadequate. Sharp CMS N50CD midi No display illumination and erratic CD drawer. CD draw motor drive band accessible via hole in carrier when half open/half closed. Use hooked probes to remove old and intrioduce new drive belt. To save dismantling all the main board to get to the CD display bulbs. Fed 2 12V small bulbs from the supply to the tuner display bulbs and illuminated through the pins to the LCD display from the top edge. Similar for the tuner LCD but as pcb is easily removable pushed bulbs under the outer edges of the display and glued all 4 in place. Sharp GF570E Ghetto blaster Neither tape playing The drive pulley tyres on both tape units were split and missing Sharp QT 250 portable stereo Intermittant loud oscillation like mains hum on one channel A nasty fault as you first think a break in contacts on the R/P or function change switch.These ok so perhaps one channel down on the SIL dual op/amp but ok.It was either the tiny 470uF supply smoothing cap to the op-amp that was intermittently causing problem. Plenty of space to replace with more spacious cap. Also replaced the feedback 33uF cap around the op-amp with a lower value as the principal frequency of oscillation was perhaps 10 or 20 Hz. Sharp VZ1560 music system One channel gone,mains hum power with button on or off. Owner fiddling with speaker wires had knocked out half of the STK4332S successfully replaced with a STK4332. The ZIF ribbon socket on the power board is the push to pcb to release type. Sony CDP M29 Tuner losing memory so replaced the malfunctioning .022F capacitor with a larger one on the other side of the pcb ,cutting away part of the shielding plate. One of the tape function keys sheared off so remade with cable-ties as in tips files. Sony CFS 210 ghetto blaster Audio fades after 1/2 hour Replace LA1260 Sony CFS 220 portable stereo numerous problems Troubles due to a tinkerer messing around inside. Symptom:Mangled tape because take up spool rotating wrong way. Tinkerer had put the long drive band on so both capstan wheels were rotating in the same direction,one should be clockwise and the other counterclockwise. Symptom : Main Slip clutch,auto reverse problems. This clutch assembly has a distinctive 2 sides of a square of white plastic. When reassembling one side of this square is located between 2 stand-off parts of the back plate and not located in what looks like a matching square recess of the main black plastic swing arm. Also when dismounting ,the sintered metal bearing for the main drive shaft is not positively located in the backplate and will drop on the floor if you're not aware in advance. The reversing action in the latch section has a torsional spring that only marginally has an end retained and can jump this end lug. If the auto reverse action fails to initiate and the internal little rotating semicircular pawl (fed from the train of 4 small cogs)jumps then the carrier for this is worn loose and needs a bit of packing glued in the space between the two parts. Failure to auto reverse at one end only - the mechanism initiates and the slide activates but fails to shift the spool drive from one spindle to the other. Probably due to worn cog axles,the teeth grab on in one direction and there is not enough force from the spring that connects with the slideway to shift into the opposite position. Remove this torsion spring and reform the tail arms so that the angled returns are nearer the spiral section to bring the two arms closer together. Symptom :Tape playing warbled in one direction and ruffled tape but OK in other direction. Which ever direction the tape was playing the trouble was at the beginning that is the tape winding onto the start of the spool of tape. It was not immediately obvious but the tinkerer had removed both felt slip clutches located on the spool spindles and were missing. Lack of back torque in the tape was the problem To avoid disassembling whole mechanism made up 2 rubber washers with a felt pad between to stretch and slide over the tape drive dogs. Not matching spaces so different thicknesses of rubber for the supply and take-up sides and small enough to clear the spools of the cassette. One channel playing reverse of other side of tape due to misalignment of the linkage to the miniatute head select slide switch adjascent to the tape head. Sony ICF C600 clock-tape-radio Clock stopped with just colon displayed not flashing and no tape transport Reduced the value of the 100K resistor down to 30K that feeds the mains freequency AC signal to the LM8364 main clock IC. The cassette transistor switch activated by the leaf switch on the deck was malfunctionimg. Replaced this with a BD135 Sony HST D301 stack audio Numerous faults. Nearly all I/P and O/P sockets on the rear pannel had bad solder joints,not from abuse but poor production quality control,insufficient solder bath soldering.Squeal of one tape drive due to dirty pinch wheel and spindle . Intermittent drop out of tape transport on other drive due to out of position tape-in leaf contact switch in upper part of cassette compartment. SOSL N-X-211,Retro 1940s CD player , no CD Weird one built into a (plastic) simulated Al flight case with hundreds of real screws for effect. Cross-head not slot-head though, 40s/50s assemblers and repairmen had no power drivers and could handle screw-drivers without slippinng. 2 simulated analogue meters, black front panel, black and Al plates and white & red chequer plates, proper traditional toggle switches instead of click-switches ( the only decent bit ) etc. Opening the case there is even an odd musty sort of smell, probably the gummy glue used all over the place. To open case remove 6 long screws at rear, 2 feet and the side hinges to release the grommet material and prize apart the grey & black sections which are gummed together. Anyway probably made 1993 in China. Bass boost off and side speakers disconnected then no output, bass goes through body speakers, also no balance ,treble or bass controls. Fault Radio works but no power at all to the CD area. The CD status lamp (simulated pannel lamp indicator) does not light either . 2SB777 gating transistor not passing 15-16V to CD section. 4013 pin 12 o/p ok on CD select also i/p line to 4052. The 3.9R presumably fuseable resistor is o/c replaced with 0.5A fuse in series with 3.9R, 0.5W metal oxide. Teac AG 260 Tuner-amp Crackley volume and loss of bass. Uses a bass compensated volume pot - worn track - recondition as per tips files. Remove front panel PCB and use hot air gun to de-solder and prize-off the pot. Technics SA K2 tape,tuner,amp Intermittant loss of Output especially on power-on Corroded contacts on the phones outlet socket on front panel that switch in or out the speaker outputs. By pass the switch contacts by adding a toggle switch . Technics SA Z5L tuner amp 1995? No am or fm but aux to op ok. TO220 ps pass trannie temp affected solder. Bolted a finned heatsink using the existing heatsink bolted through trannie hole. Technics SL1210 , 1979 ? Intermittant loss of one channel. The headshell was slightly loose on the tonearm and moving inwards would cause loss of one channel. To remove this arm undo the slotted lock ring at the very top of the arm pivot and undo the central pin. The arm with jiggling can then be removed assuming enough slack in the signal wires. Undoing the 2 watchmakers screws near the headshell allows removal of the 4 pin connector. Presumably the wires inside the tone arm at this connector could touch the inside of the tonearm and lead to break in sprung connection. Placed a bit of brass shim in the slack area and pushed back in to wedge tight. Also removed the soft washer on the plug shaft of the headshell. Technics SL 1210 Mk2 ,1979 (electronically much the same as SL 1200 ) Wrong dedented speed,no stylus light and sticky / rubbing ? tonearm . On test point 27 the f on a counter should be 262.08 KHz (for 33 1/3 rpm ,/N=162 ;for 45 /N = 120 ) so 262080 = 162 X 33 1/3 X 182 (pips on platten) X16 /60 seconds. Was about 261.60 KHz. Green LED on dedent lights on speed lock and strobe freezes large pips on platten periphery. Stylus lamp was blown 20V small filament lamp ,filament not ideal because of percusive nature of the pop-up action plus unavailable 20V. Placed a slab of rubber loosely around the microswitch latch assembly to cushion this judder when the lamp assembly hits top. Replaced with 3 slab type LEDs soldered in parallel and ground down edges and front faces to feed into the Ali slot. Bed in with mastic or "blue tack" to position and glue in with hot-melt. Run from the supply with a 200 ohm,2W R in series. A better solution would have been a high intensity 'key fob' blue 3mm LED and 470 ohm bent , wired and insulated as a replacement, I've since used on other 1200/1210 decks. Checked pivot adjusters, lock nuts had "loctite", so heated with soldering iron to free up. Problem was probably crossed turns of the hair spring torsional spring for the anti-skate mechanism. To remove tonearm (first remove headshell and cartridge) and set anti-skate to zero. Undo signal lead clamp and all screws from the underside of the mount (including under the terminal board) except one nearest the vertical pin that is touched by the anti skate spring. Tie cotton to the fine signal leads before extracting. Technics SL 1210 this time with guillotined lead to the stylus illuminator , no green LED on dedent position of pitch slider pot The silly ring of soft plastic around the brass barrel had broken allowing the slide to go far enough to cut the wire to the lamp. Also missing tonearm lifter lever. Found a length of brass hex spacer threaded 3mm one end and tapped 3 mm at the other. Broke up an old standard size paddle toggle switch for the plastic paddle. Heating with low setting hot air gun melted an angle into the pivot area and tapped a 3mm thread onto the switch end of the paddle. Screwed into spacer and screwed other end of spacer into the horizontal rod of the tonearm lifting mechenism. LED problem due to o/c switch in detent f lock position. Nothing done to rectify as owner content with knowledge only cosmetic,this switch is built into the slider pot housing. Technics SL1210 Broken power switch. They tried being clever but too complicated. The shaft of this mechanism passes through the LED strobe housing. The brass shaft is not mechanically held to the knob positively so breaks away and shaft drops internally. Replaced the 'cam' bit that activates the microswitch with a brass cored plastic knob. About 12 / 13 mm diameter ,replaced the grub screw with a bolt . Due to it being a standard 1/4 inch knob and the brass shaft being only 4 mm or so when fixed against the flat the knob is off-centre so acting as a cam. The flutes on the edge of the knob were useful for feel as well. Added a bracket piece to form end stop for rotation by hitting the extended bolt in the knob. Technics SL1210 Mk 2 , 1983 Non-technical owner had service manual and tinkered inside and managed to blow up the power supply. Main pass Tr ok but had to replace the 2 2SD637 with 2N3904 with swapped legs. Also the 5.1V zener had gone ohmic and replaced 400mW with 1.2W. Main crystal osc. locked on f, all 3 drives to platter are working and once settled at 33 or 45 RPM it all stays locked into speed strobe. Always from start or from 33 to 45 locks in quickly but sometimes , about 1 in 3 times going from 45 to 33 will take 2 to 4 seconds to lock in to lower speed. Rarely will the brake properly fuction ie stop between 120 and 270 degrees after stop signal at zero degrees, usually continues jerkily faster than 45 rpm until the power cut ,time-out, after a few seconds. Makes no difference to the jerking what setting of the brake adjustment pot. Adding the heavy rubber platter mat does not damp things and improve matters thinking some servo gain/resonance effect. To monitor voltages needs small hook probes and wires fed through the illuminator access point or bottom and top halves of unit unfixed. Seemed a problem with the section of the AN6680 custom IC that outputs the braking signal to the drive IC. The main f oscillator section is fine. This errant section gates the 33/45 switch and start/stop switch. Should output 1.5V in run and 0V on braking but in the non-locking 45 to 33 changeover and lack of braking situation it is outputting 3 to 4 volts. Added a 1.5V zener and a 2.4K limiter across the capacitor connected to AN6680 (21) / AN6675 ( 22) trace. An ongoing problem, not explored as minor, is unit needs switching on 3 minutes before rotational use. In those 3 minutes perfectly useable but only 99 or so percent lock to speed. In passing, placing a 1K across C214 100uF cap so simulating a leaky cap produced highly errartic forward and backward rotation. Whether would happen in general case or just because of the fault in AN6680 , i don't know. Pitfalls 1/ the index 'pip' for positioning the bearing into the base is not at 12 o'clock but 4 o'clock position. 2/ convenient earthpoint is ps pass transistor clip but that needs earth continuity via one of the PCB mounting screws in place. 3/ With upper cover, under platter, removed to work on it, is possible with fingers in the platter to place/remove, it is possible to touch live mains components. Technics SL QL1 radial linear tracking vinyl deck, 1981? Perished "rubber" mat. The 3 small radial slots either side of the mat line up with the 3 LEDs under the platter and 3 receivers above the record/platter and also holes in the platter so matter of cutting holes and adding rear locators to the mat for alignment. Marked positioms , sewed some loose thread into the rubber and filled with hot melt glue , then repositioned, marked for the 6 small holes and cut with leather punch. There are 2 VR accessible via a rear plate but presumably 33 and 45 rpm adjust. So just masking off them and taping down the cover closure microswith allows exposed to work on in operation. If hares away then platter has slipped from near hall effect sensors. 2SC1846 5,12,5.7V 2SC1846 12.5,22,12V in operation ( 2 tight grommets over spindle to allow use upside down) CN304 9.4,.15,0,0,6,3.6,0,5 305: 5,0,0,3.5,3.1,0 302: 11.7,5,0,8.3,12V 305: 1,0 301: 0,3,0,0,0,0,5,1,12,0,0,0, Technics ST-600L Intermittent loss of display. Replaced the on/off switch but on replacing noticed the problem may have been due to a broken pcb track as switch not mounted to chassis but straight to pcb so strained if heavy handed. For the extended stand-off removed one switch from a ganged array and wired the latch to the body of the switch Toshiba SR-B30F deck Twisted and bent 63M cartridege stylus shaft.. Pulled out with no more than fingertip pressure and again with fingers only as a hollow aluminium shaft, bent back straight. A spot of glue in the housing and replaced Trio / Kenwood KB 1022 record deck Platten rubbing on chassis. Also the new owner did not realise the speed change lever should be returned to neutral midway position in play. Undid main spindle nut to remove spindle. Removed small screw to disassemble and cleaned out with meths. Dropped a small washer into the housing then the ball bearing. This raised enough to let platten clear the deck. Trio / Kenwood KR 2010 Tuner-amp On one channel sound ok on phones but distortion on full load with speaker. One of the pre-driver trannies was partially O/C all 4 power trannies ok

Cassette and Tape players

Sticky dampers on cassette flaps The compact dampers based in a cog that supplies friction against the spring action.The construction of these is 5 or so concentric rings engaging with a matched set and friction supplied by silicon grease which can go viscous with age so wash some of the grease out with methylated spirits Aiwa AD1800 1972 tape deck Broken main drive band preceeded by intermittant aborted play/record. Remove top cover by sliding to the left and unclip. Remove 6 screws from the base . To remove front panel remove 6 more screws 3 machine and 3 tapered. The main drive band has to be wide enough as well as right diameter or it will ride on the balluster pulley . The "running" light would stop soon followed by drive stop. This is fed from the hall switch near the tape counter which had moved away from the magnets so moved back and anchored. Also slipping drive bands replaced between take up spool and counter. Second machine same model. All belts perished,no transport. To remove the cassette carrier remove 1 circlip and extract the black pivot rod. To get to final counter drive band remove the 3 screws that bolt this sub-assembly to the chasis. Remaining belt exposed by removing flywheel remove circlip to pivotted arm . Replaced pulley tyre and the associated band. Bulbs probably 6V driven by 5.3V ac. Aiwa AD 6900, 1978 tape deck Cassette play drops out after a couple of seconds. Not made for maintainence or repair. To get to mechanical deck requires removing front panel and 3 headers to remove through sub chassis. Then sub chassis requires 2 screws removed either end of monitor & tape select switches. 3 screws mounting large solenoid to base. Unclip shaft and remove mains switch. Remove left-most vertical pcb. Remove tape counter band . The 3 meter function select sw extenders are very weak at junction of clear and chromed plastic. Remove the cassette deck back plate and surround plastic trim. 2 screws were too tight to unscrew and needed grinding off. Remove sub chassis , numerous peripheral screws. To replace spool drive band remove the 3 screws holding the white pulley and slip clutch assembly and joggle band around the end of shaft. Drive problem had probably 2 causes. The take up spool brake rubber had part broken or deflected allowing the arm to rise too high and fouled the jockey assembly so high speed spool drive part engaged in play. In play the sliding jockey was marginally touching a 2mm drive shaft. This was probably covered in a plastic cylinder extension from the main FF section pulley. Interference fitted a 4mm brass cylinder over this 2mm shaft. Also made a bracket to hold back the top position of the spool brake. The supply side felt brake also needed attention as thin and polished. The sliding jockey assembly must not have too strong a spring to engage as then the whole play sledge plate will not reliably disengage. Finally a clicking noise from the take-up spool. The spring immediately under the cassette engaging drive dog was compressed to solid and the plastic piece needed pushing back to compress the conical spring to bring the counter band into alignment. AC voltages at fuses in play mode 11.5,25,16.5,16.5,8,16 Voltage to deck illuminator bulb is 7.5V ac Aiwa AD 6900 Mk2, 1979 much as "mark 1" but added sensor and board Similar lack of drive due to perished rubber parts. These things are designed to try the patience of a saint. Everything requires something else removing before you can get to it and nothing is self-aligned before screwing back together again so before undoing a motor or tape deck or whatever mark around it with felt tip pen, especially the solenoid mounting plate and the isolated screw through an cartouche-shaped slot underneath. Reassemble this last so that the obvious play/disengage slide works but also the hidden secondary linkage that operates in reverse sense to disengage brakes and lock the FF/REW pulley in central position play. Jiggle around this mounting plate , slightly lifting and dropping into the hidden locating slot. If in wrong position, the hidden slide mechanism fails to operate and you can get fast and play modes operating at same time and tape pulled through capstan gate. Disassembly as other 6900 above, keep sub-section screws in labelled bags. Deliberately made awkward, the slip clutch spindle bearing mount could have been rotated 60 degrees so not difficult to undo the bottom screw. A slot could have been put in the front sub chassis plate so the wiring to the 1/4 inch sockets could pass through to give more space to release the deck section. I still don't know how one is supposed to remove any of the 3 off 1/4 inch front sockets for replacement. Each seems to be pushed through a hole (not two-partable sections ) and then held in place by pushing a rigid plastic ring over the barrel and locking under the frontmost lip. As this plastic pokes through to the front I don't know how you're supposed to remove it un-butchered - hot air gun softening ?. Otherwise requires a source of large LED mount back ring/locks to replace butchered originals. ? Cut down BNC socket cable entry protectors cut down and then body of socket glue in would probably work.To remove the play mode slip clutch spindle as above. To totally remove , first remove the take up spool then remove the slip clutch pulley from the pivoted arm. Pull out and down this rear clutch section to give space to remove the other clutch assemply. Replaced that 0.65 inch tyre with an O ring and smaller packing O ring giving 0.67 inch. Don't know what the tyre diameter on the front removable sliding arm is but this had perished to a rough 0.71 inch,0.76 inches is too small , replaced with a "O" ring that gave an outside diameter of 0.75 inches. To do this with a standard 0.675 inch by 0.1 inch, wound ten turns of 2 thou plummer's PTFE around the pulley before fitting the O ring, remove the excess PTFE to avoid snagging. I know not of a source of small diameter but radially wide pulley tyres so interference fitted a piece of brass 0.3 long and 0.135 inch diameter on the play drive shaft that engages with the sliding pulley. Replaced all other drive belts. Main capstan belt requires removing the back plate to the spindle. That damn solenoid linkage fouls onto everything unless you reposition it and the solenoid last, despite having to do it totally blind. Even replacing the main capstan belt would be easier if those 3 flimsey switch extenders were easily removable whithout the glued in lock plates. Used a dentist's sickle probe to excavate the glue and then prize them off. Don't remove the screw accessible inside and thread pokes through base plate that holds down the capstan motor unless you really have to. To replace the back retainer to the capstan spindle hold the "nuts" with the sickle probe, rotating with a small screwdriver. Remove the counter mechanism to check the drive band is in correct position as cannot see otherwise. Replace the four switch extenders last and also the plastic fairing around the cassette flap goes in after putting the front cover on. Tape remaining lamp supply measured at 7.5V, replaced with 8V, 0.06A bulb Aiwa AD 6900 Mk2, 1979 R/C tr uses 4028 and M58484,and rx LF357 4558 555 This deck stopped responding to the r/c. Transmitter was ok , receiver diode ok but nothing coming out of the first op amp. The o/p is dc coupled to the next stage. The DC at the op-amps was 8V. Replaced the LF357 and m/c works all functions but only in subdued lighting. If room light is too bright then there is not even manual control of the deck functions let alone the r/c, kill the room lighting and normal service is resumed. Fluorescent light was the problem , exploring further. No room light CFL and shining bright torch at the sensor does not affect the function control but rapidly moving the torch back and forth can set it off. In that state a continuous 1KHz pulse train positive going on orange and -ve going on green until switching off and on. Seems as it was an early IR r/c it just lacks discrimination . Replacing Cs 4558 and 555 made no difference. Its not used with a flourescent roomlight but if it was then a matt black rubber cone over the sensor boss would allow it to be used. Aiwa AD F410, 1993 Warbling tape play. Seemed like a good design for changing belts etc. 4 screws to remove the deck from front. Pinch wheel unclips and 2 screws removed allows to remove back plate and main belt slips through gap under the pcb. Not a belt problem, speed warbling, too much take up (TU) tension. With hindsight the TU spool will disassemble with finger pressure but it seemed one piece construction with the counter pulley, pack out with large nut , say, around shaft and use a blade to prize off. Access to slip clutch otherwise is through the deck side , not motor side. Mark sections before dissembly. Remove thin stainless steel plate between the "2" pinch wheel holes. TU side unclipped then S (supply ) side ,reverse on assembly. Beware of small BB under this plate. By joggling the 2 sliding plates will come away. Small spring to top and larger spring to lower plate. The 2 white trigger arms , the one that folds back around the pin is the TU one. For reassembly tie both these arms down in place with PTFE tape stretched right around the deck , remove after putting plates back. Same with holding BB in place until cover is back. Replaced the existing slip clutch spring for a lighter one. TU drive in play needs the pinch wheel assembly in place. S side solenoid activates play drive and TU side one for FF,REW. Then too much braking on the S spool when a lot of tape on the spool so changed that spring as well. The spring end extension under the pinch wheel was bent so too little pinch pressure as well. Beware there is no screened cable from the tape heads and don't power up with the ground wire disconnected. If no earth then a curious distortion takes place, semi-random bursts of fast decay high-f oscillation pings or tings overlaid on tape signal. Aiwa AD F770 , 1985 Semi professional deck that uses "3 heads" so record monitoring is via separate play back heads, not off the direct signal feed. So VU / PPM only indicates in record after the tape has gone from leader to ferrite. Uses a second tape guide in association with the "reverse" downstream pinch wheel and spindle for better alignment and also paired up pinchwheels (not for any reverse/ loop play function). Apparently improves registration over the head and so more reliable high spec performance. double tape guide
Perished belts and prior to that erratic FF and REW and poor eject. As received the cassette would not eject as in tape play position when band broke. Engage the centremost solenoid while turning flywheels to disengage the slide. To remove the deck , remove mains switch bracket, cover the pcb directly behingd the deck with plastic to avoid deck catching on it. Remove 3 internal screws and one from underneath to release the deck. Bad REW/FF due to slip clutch under the deck cover plate. Remove that pivotted plate and top cover - remove the facia then prize away the 4 brass engagement nibs. Mark parts before removing innards
The sliding head mounting plate needs the retaining strip removing and then lift and angled to remove and replace, no hidden balls under this top slide. Turned the pulley tyre inside out. Poor eject due to thickened grease on both the pinch wheel carrier posts not allowing the head carrier slide to drop into eject position. Note position of springs especially the downstream one with 2 opposing springs and clean out all grease. 220mm long second band kept falling off, 250mm is too long , 230 mm belt also sometimes fell off. This deck uses double capstan drive and not much stops the second band falling off. If too much tension to pull the belt laterally one way more than the differential force to ride the hump on the pulley then it will fall off. Glued thin celluloid discs to each of the flywheel/ pulleys. This deck in record , monitors playback, rathe rthan direct from source so nothing on VU or PPM meters until end of leaders Aiwa ADWX999 cassette deck No tape functions on one deck. The motor had broken.Replaced but to reassemble, also for just changing drive band . Loop the band around all 3 pulleys and then with 2 pieces of thread at either end around the solenoid and through the rubber band tie tightly into a knot to give clearance for the motor pulley.When reassembled cut the threads and remove remnants.The motor speed adjust is not in the small hole in motor casing but on the adjascent PCB. Before replacing bands make sure the mechanism is in neutral, ie no power take off engaged by powering up and turning pulleys. Akai CS F11 audio cassette Very weak REW and FF one of the motor driver transistors marked 1012 was blown. Also 2 of the preceding trannies marked 808 were blown. Replaced the 1012 with 2N2222 with 2 pins swapped around and the 808 s replaced with MPS2907 also with 2 pins crossed over. Akai CS 702D tape deck, 1977 Intermittant no rec on 1 channel Swithc problems the main 14 way R/P switch and the rear line/DIN switch. Renovate as per tips files. Reassembling R/P switch force back the spring a bit before closing the tinplate shroud. The rear switch can be forcibly removed , bending the pins a bit, without dismantling whole deck. Ball mill slight grooves on upper face of the pcb to make re-assembly easier. Blaupunkt London SQM 37 Tape rejected after a couple of seconds Firstly removal of front pannel knobs to remove pannel and then tape deck. The volume knob ;2 thin spanners or similar cut plate one against the pannel for protection and the other to lever between knob and spanner as vacuum seal between knob and shaft,the 2 small knobs need the clips depressing at the rear of the pannel before puling off. The fault was caused either by the microswitch trigger that senses the tape carrier in play position out of position or wear on the main mechanical latch.This latch is much like a conventional mousetrap and the lip that holds the main arm when the solenoid is powered was worn so ground back slightly with a smal grinding wheel. Golding 602 8 track 1 channel o/p only One of the 2SC1013 running hot but it was the 2SA623 of the pair that was about 5 ohms between C-B. These Mitsubishi trannies have most unusual pinning C-B-E. Replaced the A623 with TIP32 with one of the legs crossed over to match BCE to CBE. The 2SC1013 out of cicuit was about 15M between B and C replaced with TIP31 reconfigured. Japanese 8 track tape Marked JS-1 on the pcb. Sticking solenoid action disabling track change and bent leaf switch disabling startup. JVC CD1740 tape Drive band slipping. It seemed there was an impossible "operational window" between a band tight enough to not slip on the drive pulley and too tight it disengages the driven pulley from the take-up spool. This driven pulley is on a pivot activated by an arm and a torsion spring to hold it against the spool. Slid a tension spring over this arm and anchored off on the chassis to give more "torque" JVC KD D30 Cassette tape unit No tape functions It looked as though the motor had failed in that disconnecting and putting a meter (low load) on the supply to the motor showed 12 volts.With motor connected showed about 2volts across motor.The low side of the motor is principally via a leaf switch on the deck which was failing to close on tape functions. Bent back the static leaf and reinforced the outer edge with hot-melt string. JVC TB W11 Tape deck. No mechanical functions. Voltage regulator excessively hot due to the motor taking excessive current although not seized.Replace. JVC R-S33 1981 Distorted sound on one channel on low to mid volume ok above that. Sounded like offtune radio station. Infuriating fault to track down. By isolation and monoing signal and checking backwards from power amp. Eventually traced back to the balance and volume sliders. Balance central and commoning both vol pot o/ps to Left op was fine on both channels commoning ops on right slider then distortion both channels low vol. Isolating this pot seemed fine with DVM resistance. Breaking open there was some gunge between part of resistive and conductive tracks having a capacitive ? effect. Cleaning and replacing and distortion gone. Kenwood KX W4060 Both decks tape jam ,nasty clicking noises and chewed up tapes Gummed up slip clutches whether from someone spraying something in the decks or as it was a white deposit if it was migrated over ample white grease gone funny. Also the smaller drive belts may have slackened and as the stretch in these is the return action of the pivoted cam plate could cause problems.Also the leaf switches are very flimsy and one was intermittant.There is a resistive coating to the contacts so not 0 ohm.To get to slip clutches:mark relative position of pivoting cam plate relative to the locus cam cog before removing. To check the decks removed from the m/c activating the solenoid from neutral position is first play then fast then neutral.For reverse play longer pull of solenoid from neutral but if not long enough then reverse head and pinch-wheel engage but forward take-up spool engages. The ribbon cable connectors are disengaged by prizing the end clips outwards to release the grip to move towards the ribbon.Use the edge of the pcb as a fulcrum for a small screwdriver to do the prizing. Kenwood X85 Tape unit Broken drive belt Have to disassemble the eject arm and remove the tape mechanism and desolder the 2 long connector pins to the solenoid not the shorter hall effect sensor pins to gain access to the complete belt path. Matsui STR626 Another burned out 9V motor. Replaced with a 12V motor ,but disconnected the pcb mounted speed monitoring section and added a 10K multiturn trimmer NAD 6325 cassette Intermitent failure to play and dropping out when playing. Corrosion on the contacts that sense tape-in, second from the left edge. Cleaned this and the adjascent one and the deck-slide in contacts on the deck area. Panasonic RQ SX10 "walkman" No play function Stretched belt not giving enough torque to the head activate / change mechanism.To gain access,remove outer casing,screws holding the pcb,unplug the head ribbon cable from the pcb socket and desolder at 6 points-3 on tape in / type leaf contact connections,2 solenoid pins and one battery connector. Hint for dealing with these pesky things,because of the watch size screws etc do all disassembly and assembly in a high sided tray to catch any dropped parts. Pioneer CT 70R cassette deck No play or direction reverse function Remove tape deck unit from chassis.Remove the illuminated back plate to the cassette carrier.A yoke made of cast junk zinc metal had sheared where the pawl engaged with the cam wheel. This material fractures with a characteristic granular structure and as far as i know cannot be sensibly repaired.Beware of losing ball bearings when dismantling. Pioneer CT200 Tape deck Incomplete erasure and low level of record signal. Bias oscillator (in can) failure due to partially shorted turns on the transformer,trannies ok. Realistic SCP 32,tape player of 1990 ? plays only but has reverse play and continuous play. Nothing after being dropped. The secondary wires on the transformer had broken held the core back in place with cable ties. Repairing audio cassette tape carrier catches. The latch arm that holds the cassette carrier against the deck that often breaks with hamfisted use and other inaccessable catches.The problem with bonding these catches back is they require fairly accurate alignment in X,Y and Z (in scope sense) while usually inaccessable in the closed state.Using hot-melt glue "string" (see tips file) with a small spot glue the active pawl end of the arm around the nib on the cassette carrier / door. Bury in this dot of hot melt a 1/3 Watt resistor low ohms (vary to suit any available power supply) with fine wires soldered to power up later to melt the glue.It may be advisable for X-sense positional latitude to temporarily place a washer on the nib. Loop some thread around the eject arm to be able to pull on when the flap is closed.Tape a thin strip along the upper edge of the door flap to give a bit of Z-sense latitude.Melt some hot melt on the interior end of the broken latch arm and the corresponding area on the deck mechanism,close the flap and wait 10 minutes for the glue to set.Putting current through the resistor and maybe assisting the eject mechanism with the loop of thread should let the flap open.Clean up around the nib and reinforce in area of original break with extra glue and maybe small bits of expanded metal. Rotel RD251 Cassette tape No FF or REW Someone had sprayed lubricant on the main drive belt, so had reduced the reactive force aganst stretching to that of a band of 1/4 the thickness.The logic must go sommething like : the tape is running erratically so something must be sticking so lets lubricate the moving parts.Washed all affected parts with methylated spirits.Access to the band can be obtained by removing 2 of the 3 most accessible screws on the flywheel retaining back-plate and flexing to leave small gap. Rotel RD500, 1981 Mk 2 No take-up spool drive Broken secondary drive band. Requires taking deck apart. Front from back and also whole deck from chasis and as poked through opening a matter of removing mains sw sub- panel also. Remove main drive band to access secondary band - 2 cogs one way and one counter direction. Mark path of the Rec string and solenoid coupling before removing. 24Vac and 11.6V ac from transformer 24V dc on ps pass tranny heatsink Rotel RD500 No tape functions Stretched main drive belt.The protruding cover to the tape head area is only held to the front cover with 4 1mm plastic lugs.Either end of the underlying metalwork has a hole either end which can take a selftap screw through the platic cover to anchor down Rotel RD500 Cassette deck. Jamming of front panel buttons Cut two strips of plastic from an IC storage tube,one flat the other L shaped in section and glue either side of buttons,parallel,to constrain the buttons on the inside of the housing. Samsung SV627 / SV827 Poor rewind and intermittent sections of lower pitch sound recorded on tape. Poor rewind referred to on tips files for "always laced" vcr problem. To record as lower pitch the tape must be slipping through the pinch wheel or pinch wheel speeding up. The top sintered bearing on the capstan spindle was worn so replaced as per tips files and motor bearings. When reassembling the capstan "motor" make sure the hole in the sub - pcb matches the hole in the metal chassis or connector will not align on reassembly. Sanyo M-W1L Sluggish tape transport. Replaced both stretched drive belts and rebuilt mains inlet socket and a case retaining screw spiggot on the case-back ,both sheared due to impact, using hot melt glue ,see hints & tips. Sony cassette player CFS903L Forward and reverse heads acting concurrently Linkage to head forward/reverse switch very puny so broken + worn belt Broken jockey/idler assembly failing to trigger end of tape mechanism. Sony CFS W401 portable stereo Deck B defunct,deck A intermittant failure to play. Deck A problem due to flimsey metal linkage between the play button and the pcb mounted switch.Bent back to shape and reinforced with expanded metal and hot melt string. Deck B burnt out internal controller in the motor due to excessive bearing friction.Replaced with exactly same make and model number of motor but poles or tacho characteristics different so ran too fast. Had to add in parallel 1K resistor between A and B terminals and change the pulley to a smaller size before in capture range of the main pcb normal speed pot adjustment. Sony DTC 690 DAT Mangled tape. Placing a force guage on the 3 wing coupler of the tape spool engagers there was just 60gm on the supply side and 55 gm on the take-up. Take-up reel has the stouter of 2 springs loading the slip-clutch. The drive voltages in different modes to the motor agreed with the manual. It seems a lot of Sony kit ,including cam-corders ,that use these low RPM motors (low audio noise ?) lose magnetism or some-such, so start-up torque and drive torque is much reduced. Also the supply side sliding tape guide was not fully retracting so snagging the tape when ejecting the cassette . Taking the relevent boards apart does not disturb any mode-switch alignment. There are 2 slots in the slide bar ,one supply side,one take-up side. Cut down a couple of small nylon cable-ties to give a 2x2x4 mm L ,side section, plastic to glue into the ends of these slots to take up the slack of the sliding guides. The main problem was loss of magnetism so loss of torque in the reel drive motor. Low rpm so low audio noise presumably. Gave up at that point but considered trying taking 6V supply or something dropped from the 12V supply to feed the 2SB TO220 trannie of the reel drive variable supply. The drive voltages were correct and plenty of current but just no torque out of the motor which did not seem to have bearing problems. Sony TC FX30 Tape Deck Play function engages 5 to 10 seconds late. The play function trips on pressing key but the cam slowley rotates.Part of the associated mechanism is a long lever on a steel axle where unnecessary grease had hargened or reacted with the plastic to bind on the shaft.Dismantle and clean out. Sony TC FX44 No tape play, FF/REW ok The pto mechanism off the capstan used to engage slide mechanism was jammed so lower of 2 solenoids could not operate. Assumed due to wide band so replaced. REmove baseplate to check this solenoid and mech. To remove whole cassette carrier remove the front panel and release the remote socket to expose the screw that holds the left hand small steel plate that limits opening of cassette flap. Then can slide leftwards to remove off pintles. One of the flimsy bits of plastic holding one of the plastic "springs" thatpivot and hold tape against deck, had broken. Wired a loop around the pivot and out to the front via 2 drilled holes. Sony TC FX44 "Motor-boating" noise recorded intermittently on one channel. Same defect can be simulated in record mode by removing the cover of the relay and lighly depressing one of the made contacts. Replaced with a sealed DIL DPDT relay but this had a polarised coil so had to cut the traces to the coil and reverse the wiring. Sony TC FX66 tape Severe low frequency distortion (motor boating) on one channel on recordings but no indication on meters during recording Failure of one set of contacts in the Play /record head select DIL relay. Sony TC FX66 Loss of high frequencies,both channels. Holding the unit while playing and changing orientation drastically altered audio output. Although the tape head was worn it was not the reason. The tapehead and pinchwheel sub-assembly is engaged in play mode by solenoid action. The mounting of this solenoid had slackened so the tape head did not enter the cassette opening fully. Sony TC FX66 Cassette tape Dead,the owner reported only the Dolby type number working and then nothing. First problem the thermal fuse in the power transformer o/c. Replaced with an external one thermally connected by enveloping in "fire cement" the stuff used to seal joints in metal-work at the back of boilers etc. Gingerly powered up but instead of secondaries of 18-0-18 and 12-0-12 it was 13-0-13 and 7-0-7 and only the Dolby light.Eventually traced the loading of the supply to the transport deck. The spool drive motor unlike the capstan drive was surrounded by thin sheet mu-metal which with time or temperature had split the cloth tape holding it in place. It had unwound slightly and was touching a component lead. Rewound tight and fixed with a pair of cable ties. Sony TC FX66 Tape pulling through capstan/pinch-wheel due to slip clutch not slipping. Even cleaning the felt/surfaces made no difference. Replaced the existing internal spring (1 Kg force to totally comress) in the slip clutch. 100 gram spring worked but not full tape length in FF/REW, put in a 300gram one. Deck bulb supply with bulb load 4.75V. Spool rotation sensor is this bulb interrupted to a light sensor on deck. The back plate , in the cassettecarrier, is vital to this operation to conduct light and must be replaced for deck function checks. Sony TC U5 cassette Main drive belt falling off . An era when SONY used good enginering but used plastic pillars to mount the drive motor. Over time plastic had creeped allowing the motor axis to drift and the drive band lie to one edge of the capstan pulley rather than central. Packed out the relevant pillar with a washer. To remove capstan pivot retaining bar you can undo just the one screw to release enough to remove drive band. Sony WM R202 recording walkman Numerous problems due to being dropped on corner nearest volume control. The machine would work with rubber bands all around it holding the battery compartment on,the cassette in and the play button depressed. To gain access undo the volume dial with circlip pliers in holes and when inside remove the reel nearest to the stop button.When reassembling outer casing beware of snagging the ribbon cable that goes to the head and the erase magnet actuation lever. One of the ends of this lever had jumped so one magnet not engaging and so incomplete erasure behind recording on one channel. In reverse play direction there was a rubbing noise this was due to one of the plastic cogs rubbing and the axle needed bending back slightly. One track inside the volume pot was broken so wired across giving maximum level on one channel instead of nothing.The pawl on the cassette flap would not engage and the other end of the actuator lever was bent and fouling the latch so not holding in in play mode. The plastic lugs holding the battery compartment had sheared off so fashioned functional replacements from small solder tags glued and screwed external to the casing. Tape decks in general Recording of a noise like old scratched vinyl records even onto pre-recorded and record protected tapes and even tape players with no record facility. The click noises are constant with a repeat rate of the speed of rotation of the pinch wheel.Minute magnetic particles have got embedded in the rubber of the pinchwheel and laying a "track" over any tape. Replace the pinch wheel as probably too soft to be cpermanently cured by cleaning. Technics M235X tape Only REW tape function Other functions lead to start / stop continuous erratic behaviour.There are 2 springs that engage a Y finger to disengage the main tape deck slide mechanism.One of these springs was to weak to properly function.Also break in 2 of the leads in the flexible inter-board connector so syscom was not recognising 2 of the limit leaf switches. Technics RS CH770,1966 part of system with ST CH570 and SE CH570 No tape transport - perished small guage drive bands. To open flaps unpowered trip the latch upwards along the edge of each deck. Unclip front section from rest of unit to undo connection between both and lift the retainers to remove the ribbon lead. Desolder each of the 4 motor lines and remove main pcb. Undo plastic backplate and tinplate screens and unclip the fine ribbon (for the head) housing , before removing motor section totally. Fine belt needs pulling off around the locus cam follower and grease removed from new thicker band after replacing. DC Voltages on tape umbilical in Play mode, as 2 rows relative to earth point on rear -1.1(12 ac),-.7,-1.1(12 ac) , 1.5,-.3,0,0,0 3.6,3.8,-.3,1.4,-.3,0,0.4 Inside SE CH570 umbilical as 2 rows -.9(12 ac),-.7,-.9(12 ac), 0,4.3,0,0,0,-.3,-25 -.3,0,4.6,-.3,4.6,0,0,14.7,0,-25 and on RSN 35H1 0,35,-35,0,14,0,-4,-14,0,0,0,0,0,0 The main belt path is the one closed to the front. The other will work but will rub and maybe squeal on part of the mechanism Technics RS M235 Intermittant lock-up in play mode. Curious fault condition where good engineering and high quality control meets a design flaw.The main locus cam cog is driven by one of two smaller cogs of about 40 teeth the profiles match too perfectly. When this cog train disengages it is not in a pure radial direction there is a partial tangential relative motion on separation.It only requires 1 tooth (so 1 in 40 occasions on average) to be slightly imperfect and while one tooth disengages ,the tip of the adjascent tooth can engage with the face of its matching tooth on the other cog and lead to a jam.So ground down all the tips of the teeth on both small cogs by a depth of about .5 mm. Technics RS T130 twin cassette deck Play deck no play or REW,record + play deck intermittant tape wrap around pinchwheel. This is probably a stock fault after 10 years of use especially as otherwise well looked after machine. Probably the same fault on both decks. I will first describe the remedy for the rec/play deck as this would only require a simple modification to rectify if caught in time. The slip clutch in the take-up spool had become too tight giving too much back torque so the drive pulley in play mode would slip. Remove the circlip on top of take-up spool spindle and replace the interior spring with a shorter/weaker spring. Attached to the head carrier slide is a spring attached to the final play mode drive pulley. Replace this spring with something a little stronger or reduce the length of the existing spring as "belt and braces". Unfortunately with the play only deck it was a case of one slip clutch binding and another one slipping too much. The equivalent take up spool back torque had been excessive before inducing final failure of the drive mechanism. There is a another large slip-clutch on a 1.5mm diameter spindle. With so much back torque the brownish cog at one end of this spindle had started slipping on the pin and the gripping part of the slip clutch at the other end of the pin had split enough to break the grip on the 1.5mm pin also. Tried reinforcing this plastic disc but didn't work and had to replace with another simple disc with 1.5mm hole from some unknown other scrapped deck of some sort. With disc of slip felt rather than the original anulus of felt. The cog end - removed cog and "forged" a flat (wider than 1.5mm) on that end and a couple of roughly matching knotches on the (softer plastic) cog to give some mechanical purchase. To get to this spindle requires partially removing the motor plate and the head carrier slide. When replacing the slide make sure the drive pin to the carrier is on the correct side of the "safetety pin" shaped actuating spring by moving the "quadrant arm" that engages with this spring.. Replacing the motor holding plate requires something like a compound winding-on motion to engage the hook pieces around the main part of the housing. Finally made the same modifications as on the play/record deck to reduce the braking effect Toshiba RT 80S Chewed tape. Firstly the DC switch side of the mains inlet needed resoldering on the pcb. Replaced the drive pulley between capstan spindle and take-up spool with a 18mm x 2.5 mm neoprene "O" ring. Also increased the tension on the relevant torsion spring that engages this drive. TRIO X-5WX Tape unit High level white noise only on both channels In area associated with the HA12088 dolby processor was a 470uF,10v electrolytic that had gone ohmic. Wien or Wier 8TD3 8 track tape player. No function Sticky capstan spindle bearing due to aged lubricant and a perished drive belt.Access to spindle by removing flywheel disc and then cover plate.The electronics p.s. is powered by 2 secondary coils on the shaded pole drive motor. Diverse Devices,Southampton,England
Telephone number - the same number as it has been since 1988 but email is now the preferred method of contact so number deliberately not placed here.
I devote time each day to replying to emails.
(obscure/obsolete components,second hand test equipment, schematics etc) Postal: 66 Ivy Rd, St Denys, Southampton, SO17 2JN England There is no point in contacting me about any of the above, the repair job may have been done 15 years ago . I cannot clarify or enlarge on any of the above.

e-mail

diverse9@onetel.co.....m ( for anti-spamming reasons please remove all 5 dots ..... between co and m ) Plain text only (see below)

If this email address fails then replace onetel.com with divdev.fsnet.co.uk part of the address and remove the 9 . Please make emails plain text only , no more than 5KByte or 500 words. Anyone sending larger texts or attachments such as digital signatures, pictures etc will have them automatically deleted on the server. I will be totally unaware of this - sorry, again blame the spammers. If you suspect problems emailing me then please try using my fsnet.co.uk account.
More hints & tips and repair briefs on homepage http://home.graffiti.net/diverse:graffiti.net/




Powered by counter.bloke.com

Counter plus 1498